The first thing I did was harvest our unexpected maple coppice by the pump shack. It’s been a few years since I cut the suckers back from the old tree stump, so they were getting pretty big – big enough to start getting into the power line for the pump shack.
I cleared out all of it, including the smaller suckers. It’ll grow back, as maples tend to do, and the first ones should grow pretty straight, without having others to grow around.
The two stacks in the last picture of the slideshow above are the largest, longest and straightest ones. All the rest went onto the branch pile for future disposal.
The ones I was keeping got dragged into the inner yard, where I could work on them in the shade. I’ve been setting aside things in two piles there. One of longer, straighter poles and branches that can go into the chipper chute. The other is leaves, branches, etc. up to 1/2 inch, which can go into the shredder chute. Once I’ve got quite a bit built up, I’ll be bringing the wood chipper over to clean them all up.
The first thing to do was cut away all the little side branches and twigs.
Since these are going to be in contact with the ground, my next job was to debark them.
Which took such a very long time.
It had to be done, though. Otherwise, the maples could start growing again. Willow and poplar – the other two materials we have for this – do the same thing. In the current wattle weave bed, I used stripped wood on the bottom layers, while the rest still had their bark. Amazingly, even without contact with soil, I spotted some fresh leaves growing!
I have to admit to feeling conflicted on this job. The job itself went well; stripping the bark on freshy cut wood went quite well and was almost meditative. I still felt like I was wasting time, when I could have been working on the bed so much faster, if I just left the bark on! I’m glad I took the time to do it, but gosh, it took forever.
I started stripping bark from the largest ones, leaving the shortest pieces with their bark on. By the time I was getting to the last few, the thinner ones were starting to dry up enough that I had to use my utility knife to strip the bark off, more and more.
I’ve got quite the pile of leaves, twigs and bark started for the shredder chute!
The largest of these were going to be the vertical supports. I measure the bed and worked out that I needed 12 for the long sides. I debated whether to just have one more for the ends but decided to have three smaller verticals at the ends, slightly offset from the long side’s posts. I decided to make the verticals a bit taller than the other bed, too, and cut them to 2’6″.
The posts then needed to have points made. For that, I went into the side of the garage where we store the lawn equipment. My late brother had set up a workshop in there, and there’s still an old vice on the counter. I was able to use that – wrapping the posts with an old cloth grocery bag to protect the wood from the vice – and the draw knife. That green wood cut so nicely!!
Ideally, I would then have treated the wood with oil, or charred the points, but I didn’t have oil for that sort of thing, and we’re under fire bans. So they went in as they were.
I’ve decided to add some wattle weave on the retaining wall blocks as well. With the spaced in the old chimney blocks, it was easy to evenly space out where the verticals would go, then hammer them into the soil. I then had to re-level the edge of the bed, since critters have been playing in the lose soil. I used one of the posts to measure roughly 2 feet from the retaining wall to set the corner posts, then set a line between them. I then used the line and the posts in the retaining wall blocks to set the remaining posts, before hamming all of them into the soil.
Then I dragged over the remaining maple pieces to start weaving.
The longest ones were used up in no time. Two were needed for each level.
The verticals are roughly 2 feet apart, like the other bed. In videos, etc. that I’ve seen about it, they tend to recommend 1 foot apart. When they’re that close together, it’s harder to bend the horizontals around the posts, and they are more likely to crack. However, with them being about 2 feet apart, the narrower ends get pretty loose before they stop. I’d do one from each end per level, which meant running out of length in the middle, making for loose ends and a bit of a mess. Some of that will be hidden once the soil it returned. Adding extra length per level would be more secure and less messy in the overlaps if the posts were just 1 foot apart, though. Which doesn’t help much if the wood ends up snapping, trying to bend them around the verticals that close together. Even using flexible green wood. In fact, I still ended up snaping one, trying to secure it, so the end wouldn’t be sticking out.
I’m glad I decided to do the ends as separate little walls. I was able to use those to help secure the ends of the long side pieces.
I ran out of the longs ones quickly, and the shorter ones were too short to be able to secure them between the verticals. They’d weave between 3 posts and just sit there, loosely.
Which is when I decided it was time to harvest some willow.
Once again, this was needed to get branches away from the power line to the house. I took only the largest ones for now; the smaller ones will need to be done, but I don’t have a use for them just yet.
After stripping off the leaves and shoots, there was a very small looking pile left behind! However, several of them were more than 12 feet long. I was able to weave those in from end to end, and just trim the tiny bit of excess with loppers.
But first, they got debarked.
The kittens LOVED playing with the ends while they were being debarked, and had a blast in the pile of leaves and bark.
Once I got as much as I could, woven in – leaving quite a few shorter pieces behind – it was time to call it a day.
I’m going to need a LOT more material to finish this.
The problem is finding lengths that are long, thin, flexible and straight.
The “straight” part is the hardest to find. Typically, the branches and suckers grow straight for maybe three feet, then branch off. Or there’s been some sort of damage that cause them to grow a new “top”.
For the retaining wall side, I could probably get away with adding more vertical posts, then use up all the skinnier, shorter pieces to weave onto there.
Tomorrow, if I’m up to it, I’m going to go into the edges of the spruce grove to start hunting down some of the poplar that has regrown. Hopefully, I’ll find some nice, long, straight pieces.
We have so many willow, maple and poplar suckers that I’d hoped to harvest for this, but the majority of it isn’t actually useable. I need to really hunt for what will work.
Which means this bed is going to take quite a while to finish. Which is fine. It’s not being used this year, and will be ready for next year. I also plan to leave the vertical supports tall, so that things like hoops or whatever can be added, if the bed every needs to be covered, to protect anything that gets planted there.
I am so tired and sore now, though, I might have to take tomorrow “off” and give my body a change to recover.
For now, I’m ready to take some pain killers and go to bed!
In the first image, you can see the seedlings that need potting up. They all should be much bigger than this, but it’s just not warm enough, even with using the heater and the heating pad, in the basement.
With concerns about the outside cats potentially knocking the transplants over when we moved them out, I decided to use some storage bins to hold the Red Solo cups I was going to re-use to pot up into. They’ve been stored in the sun room all winter, so they had to get a cleaning of cob webs and whatever other debris managed to get on them. Thankfully, the old basement is where the laundry used to be, so we still have the old laundry sink that I could soak them all in, then scrub the ones with drainage holes in the bottom to transplant into. I also pre-soaked the seed starting mix with hot water, so it still be at least not cold, by the time the cups were filled and the seedlings transplanted.
These bins hold only 9 cups in them, so that basically became my default for the maximum number of transplants to pot up into. Which worked out really well. With the Black Beauty tomatoes, there were only 4 large and strong enough to pot up. With the Chocolate Cherry, there was only 5 to pot up, so they got to share a bin. The Spoon tomatoes and the Sub Arctic Plenty both filled one bin each. The Sweetie Snack Mix peppers and the Turkish Orange eggplant both got one bin each, too, with almost zero “extras” that didn’t get transplanted.
In the second photo, you can see them after they were all potted up, before I topped them with vermiculite. The potted up seedlings are small enough that I could use the lids on the bins, but I had only 2 of them handy at the time. The next photo is after the vermiculite was added. Then I got more lids for the bins from the sun room and my daughter helped me get them out of the basement. Which was actually quite dangerous. We started with me taking them through the old basement and up the stairs to where my daughter was waiting at the door, one bin at a time. She would grab the bin at the door (keeping the cats from dashing downstairs) and take it to the old kitchen, while I went to get the next bin.
The old basement stairs are narrow; each step is about half the width of a typical step. It is also steep than most stairs are, and there is very little space at the door. Which means I could only go to the third step from the top before I ran out of space. Even going sideways and carrying the bin on one arm, I couldn’t reach the door knob, so having my daughter open the door was an essential. Once she had the bin, I could go higher and close the door, but just going up and down these stairs is simply not good. I go down them backwards, like on board ship or using a ladder.
After a few bins, my daughter kicked me out of the basement and we traded places. Apparently, I sounded like I was in a lot of pain. Which I was, but I wasn’t going to say anything, since I know it’s not any better for her!
In the last picture, you can see all the bins and trays now set up on the freezer in the old kitchen. I was so tempted to put them into the portable greenhouse. The thermostat in there was reading more than 40C/104F! Pretty impressive, considering we never got above 4 or 5C today (39 or 41F). And that wind!! Yikes! The problem is that we’d just have to take them back inside after a couple of hours, and I didn’t want to do that today. We’re still forecast to have -6C/21F tonight, though we’re not expected to reach those temperatures until 6am tomorrow, and I know it will drop below freezing inside the greenhouse, even with the heat sink. They will go into the greenhouse tomorrow, after I get back from running around.
Once that was done, I grabbed a late lunch, then headed to the post office to pick up a parcel. On the way back, my cell phone started ringing. I don’t have hands free, so I couldn’t answer it. When I got home, I found a message from the home care coordinator asking about something strange my mother had told the morning home care aid about her puffer, and having already taken it in the hospital.
???
I called back and left a message telling her as much as I knew, then called my mother. I hadn’t gotten through to her this morning about her telephone doctor’s appointment tomorrow morning, so I told her about that, first. She wasn’t impressed that it was in the morning, but it’s at about the time she gets her morning meds, so she’ll be up, anyhow – and I intend to be there, too. I then asked her about the puffer. She told me a completely different thing from what the apparently told the home care aid. She also seems confused about the type of puffer they used with her while she was in the hospital, and the original type she was using before then – which she has started using now. She had an unopened refill from before she went to the hospital, and the other type was done, so she started taking it on her own. I have no idea where she had it stashed away. Then I found out she’d already taken it three times today. I told her, she’s only supposed to take it once in the morning, then again before bed. Not several times throughout the day. Plus, we already talked to her doctor about it. This was an experiment to see if it would help with her breathing at night. It didn’t, and she turned out to be developing pulmonary edema, which she no longer has after being in the hospital for a couple of weeks.
Things were still confused, but we agreed we would talk about it when I’m there tomorrow, and she could show me what she had. I then called the home care coordinator back and got her right away. We talked for a while and confirmed my mother told different things to them than what she told me. I then found out they were giving her two puffs in the morning, but not in the evening (with the disc type of puffer, a dose is one puff, while the other puffer, a dose is two puffs, which is why the pharmacist and I decided to fill the prescription for the disc type). So there’s a mix up right there, too. Not that the puffer has been helping her in any way, but a neighbour of hers has asthma, so she decided she needed a puffer, too, and the doctor was willing to test it out with her rather than go through the years it would take to refer her to a specialist and get all the respiratory testing done.
Hopefully, we will get that straightened out tomorrow.
After I was done on the phone, it was time to get out and see what I could do to protect the winter sown raised bed.
I have a cover for the bed, but it needed some maintenance work first, so I brought it closer to the garage, where my tools where. One of the things that needed to be done was secure two sections of the mesh. The jute twine it had been tied together with before had degraded and broken apart. I’d already had to replace the twin in the other join and used paracord for that, so I did the same thing again.
The hoops supporting the mesh are sections of pipe that turned out to be rather too strong. They are held in place with strips of metal strapping, but would get pushed downwards – usually because of a cat jumping on it! So I wanted to get those nice and snug, then screw them into place.
Syndol and Judgement decided the mesh was a night place to sit!
After the hoops were secured, I brought the cover over to the raised bed, but had to get a daughter to help with the rest, because of the wind. We got the cover on the bed, then opened one of the 8’x12′ plastic I’d picked up to cover it.
It was a lot thinner than I expected. Definitely not 7mm, which is what the guy looking up the information for me said it was. I suspect he didn’t quite understand what I was asking for.
Still, it will work for now.
We made sure to water the bed before putting the cover on (and I had to fix yet another hole dug into it). I noticed there are more sprouts coming up, so getting it covered to protect it from tonight’s cold will be a good thing!
After unfolding the plastic, we rolled and tucked the excess under the frame as best we could, but that wind was still threatening to blow it off. After looking around, I found a couple of sticked I’d joined with twine threaded through sections of a hula hoop to create a support for ground cherries flattened by the wind, a couple of years ago. That did well to drape across the top of the cover. We also found some lighter old boards to set on top as well; you can see the end result in the last photo above. Hopefully, it will be enough, but with how strong the winds are, I’m not entirely sure!
If it does hold out, it will protect the sprouts from tonight’s cold – and I plan to leave it on to also protect the bed from the cats! When it’s less windy, I’ll see if I can find a better way to secure the plastic, too. It’s meant to be temporary, though, so we’ll see. When the plastic is no longer needed, I have to find a way to close up the ends of the cover, so it can still be used to keep the cats out.
Since the coldest time of the night will be around the time I’ll be feeding the outside cats before heading to my mother’s, and then I’ll have to hit our own pharmacy in a different town when I’m done there, I’ll have to get my daughters to keep an eye on things and, when it starts warming up, move the transplants into the portable greenhouse. We’ll probably need to leave the door tied at least partly open so it doesn’t get too hot in there. Tomorrow’s high is supposed to be only 9C/48F, but if it could get as hot as it did in there at our current temperatures, it’ll get even warmer tomorrow. By the weekend, we’re expected to get highs above 20C/68F. Hopefully, before then, we’ll be able to get more progress on the trellis build. We’ll also have our Costco stock up trip in a couple of days.
Okay, so I FINALLY was able to work on that drain pipe from the kitchen and laundry that keeps clogging. It’s been open enough to do dishes, but from the sounds I keep hearing from the laundry drain, it seemed to be closing up again. I’d already used the snake a couple of times before, and now have the pipe cleaning brush. I just needed a time when no one used, or needed to use, the kitchen sink for a long time.
A really long time, it turned out.
So I got the coupling access the plumber had put in open, and the first thing to do was to use the plumbing snake. Sure enough, about 6 feet in, I hit a bottleneck. I punched through it, and could feel another one a short distance past it, and punched through that. I ran the drain snake through far enough that I could tell I’d gone past the bend under the bathroom and was starting to down the pipe towards the septic tank.
Then I tried the brush.
*sigh*
I got the longest one I could find, which was just barely long enough to poke at the bottleneck. I’d pull it back and could see gunk stuck to the bristles. I’d prepared a bucket of hot soapy water for this, so I’d rinse it off and do it again, but I just couldn’t reach far enough to be effective. The coil would have been too flexible for anything longer, though.
I used the drain snake again and, from the gunk stuck to it when I pulled it out, it was doing something, but it just wasn’t enough. I needed something longer, with some flexibility, but strong enough to punch through that bottleneck.
Which is when I remembered we had a length of Pex pipe left from replacing some of the copper pipes to the tub and shower.
I was getting a lot of this mud-like gunk out with it. That pipe had a thick layer coating the inside of it.
The Pex pipe had a bit of a curve to it and even that helped, as it allowed me to twist it around and scrape the inside of the drain pipe.
There was so much of this gunk coming out.
At about 10 feet, however, the pipe still wasn’t long enough.
Finally, I broke out the commercial drain auger. There was nowhere to plug it in, and this is not something to use an extension cord with, but I figured I could still use it manually. I used the spiral bulb tip that was already mounted on it, which is basically a much larger version of what the small drain snake’s tip is. It also has cutter and spade tips, but those weren’t going to do much, manually.
It worked out surprisingly well.
I reached that bottleneck and had to work at punching the larger bulb tip through. It seems like something hard is coating the inside of the pipe, there. Thinking about where that would be on the other side of the wall, it might be ice. It’s pretty close to where the old basement window is. The second bottleneck is close enough to basically be on the other side of that window, so it might be more ice. Or, should I say, frozen gunk.
We might need to look at getting insulation around the pipe in that area, and see if it makes a difference.
Anyhow.
I ran the auger through until I hit what felt like a wall. After much manipulating, I managed to get past it, and could keep going, but when I pulled it out, cleaned off the mess, and did it again, I hit the same block.
After a couple of times, when I hit the block again, I grabbed the coil right at the pipe, pulled it out completely, then laid it on the floor. I then walked along from where my hand had gripped it, using my feet to measure the distance. It was about 12′ to the end.
I then went into the old basement and, taking into account the length of pipe from the root cellar to the old basement, walked the distance along the wall the pipe runs over.
It turns out I was hitting the bend in the pipe, under the bathtub.
After wiping down the coil and bit (again), then using it in the pipe a couple more times, I finally decided it was enough. By this time, I’d spent about an hour working on it. I could have kept running the auger through and kept dragging out more gunk, but I think I got enough of it out for now.
The pipe ends needed a thorough wipe down before I slide the coupling back over the opening and tighten it down. Then I got someone upstairs to run water in the kitchen sink while I watched to make sure nothing was leaking.
Then it was clean up time.
I so appreciate that old laundry sink the the old basement!
I got the small drain snake cleaned up first, then set the auger’s coil to soak in hot soapy water – about 15 feet of it! – while I did what I could to clean the length of PEX pipe. The end was completely clogged and I couldn’t get it completely clear, but clear enough. That pipe is now stored elsewhere, since we can no longer use it for plumbing. It will be very handy again, I’m sure!
The commercial drain auger’s coil took a lot more effort to get clean, and I know I didn’t get everything off, but it’s no longer completely coated in gunk. I’ve got the coils for both the drain snake and auger coil laid out on the new basement floor to dry now, so they won’t rust when they’re coiled back into their drums.
By the time all that was done, I was feeling thoroughly disgusting. At least I had gloves to protect my hands, but I still got splattered and splashed, no matter how careful I was.
It felt so good to get showered and changed!!
For the next while, we’re going to have to make extra effort to do that maintenance flush the plumber recommended; filling a sink full of hot water, then draining it while squeezing some Dawn dish detergent into the vortex that forms at the drain. We also have some of the enzyme stuff left for weekly treatments, though we might do it twice a week for about a month.
I’ll need to do laundry but, for now, I will still run the drain hose out the front door. I want to make super sure that pipe is open enough for the water to drain through without backing up and flooding the entryway.
Again.
The washing machine simply drained too fast for the water to get through that gunk coated pipe.
When we first moved out here, my brother had moved the washer and drier from the basement to the entry for us, taking advantage of plumbing that was already there (there used to be a sink installed there). When we did laundry, we always used cold water. Partly because of the troubles we had with the hot water tank, but also to save on electricity. Thinking about it now, this probably contributed to the problem. The kitchen sink is the only other thing on this line. Any hot water from there wouldn’t have been enough to make up for all the ice cold water solidifying the gunk lining the inside of the pipe.
That’s my theory, anyhow.
So we’ll be making a point of getting as much hot or boiling water running down that pipe over the next while, with dish detergent as often as possible. If I can still hear water gurgling through and sounding like it’s backing up, I’ll have to open things up and run the auger through again a few times. Only when we’re sure things are flowing well enough will we try a load of laundry.
Starting with the hot water “tub clean” setting, first!
It will be so nice to not have to run a hose through the storm door window anymore. Especially with the inner door no longer closing properly!
Which we’ll be doing as soon as my daughter is done with the dishes.
Now, if you’ll excuse me, I’m going to give my boots a thorough cleaning…
Today, he worked on our septic plumbing again. This after already spending a couple of hours outside, doing things among their stored items, and being sick, too!
A few days ago, they’d gone out for dinner and he’d ordered a “Canadian burger”. Yeah, one of those virtue signaling things so many places have been doing, suddenly pretending to be patriotic because our government and media have told us to hate the US right now. Just a few years ago, the same people were calling Canadians who flew the flag and displayed patriotism racists and Nazis and white supremacists, just like Americans – or at least the Americans they tell use to hate. People were arrested for flying Canadian flags, banned from businesses, their property vandalized and even physically assaulted. Now, suddenly “American style patriotism” is no longer bad. Funny how easily people can spin on a dime and not see their own double standards.
Ironically, the restaurant was a US franchise.
Anyhow, the burger made him incredibly ill. He thinks the beef wasn’t fully cooked and he was hit with e. coli. He said he was still operating at only about 80%.
His 80% is more than a lot of people’s 100%, though! The guy is amazing. I don’t know how he does it!
I had other things to get done before I went back to working on the basement, so I didn’t get to help or watch while he figured out how to install the new bypass. I cleared another section in the new basement enough to mop it, then joined him after I set the blower up to dry the concrete floor. By that, he was pretty much done and ready to start testing. He was quite happy that it worked out much easier than he expected.
The pipe to the ejector now has the T insert in it. Under normal circumstances, effluent would just go straight through this pipe and to the ejector, out by the barn.
In the next photo, you can see the ball valve in the emergency diverter pipe, in the open position.
I was really curious how he would work with that diverter pipe. It had a very strong curve to it, in the wrong direction! What he ended up doing was first, rotating it so that the curve was in the other direction. Then he used his heat gun on a substantial section of it, until he could straighten it out enough that it could be attached to the T. He had to stand there and hold it straight until the pipe cooled enough to hold its new shape.
Of course, he had to cut sections out of both pipes to install the T and the ball valve.
While this was being worked on, the family was concerned about using the water. The septic pump was turned off while he worked, of course, but it had gone off not very long before he started, so there wouldn’t have been very much water in the greywater side of the tank. Any time I got a message, asking if it was okay to flush or shower or whatever, I encouraged them to use plenty of water, so we could have something to test with!
Before testing it, my brother went outside to check the diverter at the house end to make sure nothing got knocked askew while he was manipulating the pipe around. Once that was done and he was back inside, he turned the pump on manually – an easy thing to do, thanks to the second switch he installed for that! – and checked for leaks. There was a tiny leak at the elbow before it goes out of the house, so he tightened the screw clamp and added a second one, just to be safe. There was no leak when he turned the pump on again.
So we knew that effluent was flowing through the open ball valve in the diverter. We could see in the filter that water was flowing, and we could hear it, too.
We didn’t test for long, though, as we didn’t want to actually empty the tank.
The next test was with the valve closed. We were both watching that filter closely and, while there was movement, it didn’t look like it was flowing. The only way to know for sure, though, was for one of us to go to the ejector, while the other turned the pump back on.
My brother went to the ejector, then video called me on Facebook messenger, so we could see and show each other what was going on. Once he gave the go ahead, I closed the ball valve again and turned the pump on.
Nothing happened.
No flow out the ejector.
We waited a while to be sure, before I shut off the pump, then opened the ball valve again.
Which is just awesome. Without the valve, the only way to test if the ejector is working would require switching pipes – then switching back again when the test failed. Not only is that messy, but every time that is done, there is a risk of breaking something.
What this means is that the emergency diverter is now a permanent set up. Once the ejector is working again, we can close the valve, but can be ready to simply open it again, if we have more problems in the future.
We won’t be able to do anything with the ejector until things warm up a lot more. My brother thinks it’s most likely still frozen at the bottom. I think there’s something blocking the venturi valve. Worst case scenario, the pipe from the house itself is clogged, somewhere. That’s more than 300 feet of pipe, and a clog could be anywhere in there!
Either way, we won’t be able to find out until spring thaw.
Until then, the emergency diverter is our life saver!
Once the bypass valve was installed and tested, my brother headed out for home, with plans to visit our mother along the way – and bring her a hot supper to share. No meals on wheels on the weekend, so I’m sure she would appreciate it. I just hope she treats my brother well this visit. She’s really been on about how he was “keeping secrets” from her because they were so quiet about selling their acreage and moving, even though she knew that was why they brought their equipment here to the farm. I think she even forgot that they’d done that. Ah, well. I’ll find out later tonight!
I am quite pleased with how things have gone today. While I don’t have my seed starting set up in the basement yet – quite a bit more work will need to be done down there, still – I did get good progress down there, and was able to reclaim my work station. My brother got the bypass valve installed and, while we were doing that, my daughter was spring cleaning in the kitchen and dining room. She was able to get all the cat hair off the walls, ceiling, cupboard doors, the ceiling fan, pictures on the walls, curtain rods, etc. That alone was a HUGE job. With so many cats, of course there’s cat fur everywhere, but when it sticks to the walls and anything on them, it doesn’t want to come off! It won’t even vacuum off. She had to get right in there and scrub. She did an amazing job, though by the end of it, she was really needing painkillers!
So was I, by the end of it all. I haven’t gone up and down the stairs so many times in one day since we cleared and cleaned out the basements. Yes, I took my prescription painkillers in the morning, but even those can only deal with so much, and I can’t take more during the day, since I save my second allowable dose before bed. Pain is more of a problem when I’m lying down and trying to sleep than during the day. I can put up with it more when I’m up and about. Once I’m in bed, it keeps me from getting sleep. I did take some acetaminophen, though, to help take the edge off, at least.
I have a few last things to do in the basement before I call it for the day. Tomorrow is Sunday, which I try to keep as a day of rest. This will make sure I don’t over do it and put myself out of commission for days. As long as we get something set up for seed starts within the next week, it should be good. Most, if not all, of the seeds I ordered should be in by then.
From there, it’s the fun part: going through all the seeds and choosing which ones to start and when!
Today, I started on cleaning and organizing the basement.
Again.
A few years back, we were able to clear out all sorts of things from the “new” basement – the part that’s under the addition added in the 70’s. Lots of stuff went into the barn for storage until we could figure out what to do with them. Lots went to the dump. Eventually, we got it to the point that we could scrub and sanitize the concrete floor, and set it up into a useable space. We were even able to turn a table down there into a work station that I was able to use for wood carving and other general small building projects.
Then we used it as a maternity ward when Butterscotch and Beep Beep were both pregnant at the same time again.
Then we blocked off access to the old part basement so we could let the case into the new part basement. It became where we kept most of the litter boxes and and food bowls.
The cats, being cats, ended up using pretty much the entire space, as litter boxes. Sadly, that included my work station, causing damage to some of my tools, including some of my carving tools.
Then we had some wet springs and discovered the weeping tile was no longer doing its job. As water seeped through and fans needed to be set up, we had to start moving things wherever we could find the space, to get them out of the water, even though they were already on top of things like floor tiles that we found, to keep them from having direct contact with the concrete.
Eventually, we had to stop allowing the cats in the basement at all, and it’s been quite a disaster ever since.
Which meant we could move the barrier between the basements (there is no door; just a vaguely door shaped hole in the old basement wall), so we no longer have to go upstairs and around to the other door to go from one basement to the other.
It also means we have a large, cat free space.
Right now, my goal is to set up a space where I can start seeds in the last week of March. My original thought was to reclaim the work station and use that.
Well, that didn’t quite work out.
Because of how disorganized things have become, I need to work in stages, and that table was the first stage.
The table itself is a bit rickety, and has a larger sheet of not-plywood on top. After clearing the surface, I decided to take it off completely to see why the the table was so unstable.
It turned out that the surface was two wide boards nailed to the frame. The frame itself has extra cross pieces that allow for long items to be stored underneath – something I’ve found quite handy. There were still a few things under there, so that got taken out, too.
In moving the table around, I found the corners of one board were lifting, so I decided to secure both boards with screws. I used the old nails as guides on where to drill the pilot holes, since the frame they were on hid the supports they were nailed to. On one side, while drilling the pilot holes, I discovered gaps and had to drill new ones about an inch over. Then I had to add a couple more screws at each corner to secure it to the outer part of the frame as well as the supports I couldn’t actually see, underneath.
Securing it with screws did improve the ricketiness, but one corner still seemed to be lifting somehow. I finally tipped it on its side to see what was under there.
Which is when I could see just where these boards came from and, to be honest, it broke my heart a little.
Years ago, my parents bought some property as an investment. The building used to be a general store in the front, with living quarters in the back. The general store itself closed some time in the 60’s. There was a semi-detached storage building (which is now here at the farm), and I remember finding old inventory lists from 1963.
Most of the wall shelves were removed. I have a large section of one against the wall in my bedroom right now. Smaller sections were turned into dividers between the living and dining rooms. Other parts and pieces of them have been turning up in various places around the property.
The wood that was used to make these shelves is really excellent – and very distinctive in their size and colour.
The underside of the table had that distinctive colour. I couldn’t see it on the top, because it had been so scoured and damaged.
Even the larger board I moved looks like it came from this old store. Once I saw the underside of it, there were “shadows” showing it was part of something else. I even remember what it was. There was a multi-tiered display shelf in the old store, and this was the top of it.
Which also explains the cut off corners.
There is another sheet of this same wood that’s even larger that we found while cleaning the basement, and I now realize it would have been a lower level of this display shelf.
It’s such a shame that someone took apart these shelves and used this excellent wood to basically make a scrap material work table, and the surface got so damaged.
I never did find why it still seemed rickety, though. In fact, it handled being moved around quite well.
Once I had it upright again, I realized the narrower size of the table was much easier to reach around, and I considered not putting the sheet of not-plywood back on. However, my husband had picked up a huge self healing cutting mat for the work station, and it was finally going to be used – and it was wider than the table!
So, the top sheet went back on, and it turned out to be just a fraction wider than the cutting mat.
Then I put stuff back on the table, and I now have a work station again.
There is an outlet on a pillar opposite this wall and I’ve got a power bar running from there, across a floor joist in the ceiling, and a number of hooks to hold power cords up and out of the way. This allowed me to use my Dremel and wood burning tool, and now the charger for my drill and driver batteries. The power bar has USB ports, so I can set up a charger cable for my phone, too.
That top board is not attached in any way, so when it was time to put the vice back, I didn’t want it over the cutting mat. It is now on one end and holding the top piece to the table surface together. The top piece is almost exactly the same length as the table.
Before I’d put the table back and starting returning things, I made sure to clean the floor underneath as best I could without actually mopping it. I could see that the bottoms of the table legs had water damage. After looking around for something to protect them, I found my stash of old sour cream containers. I’ve been cutting those up to make plant markers, and had a bunch of them waiting to be used for that. It turns out the table legs fit in them, so we now have protection from water, if we get another wet spring.
Once that was done, I was happy to have a work station again.
However, I still don’t have a place to start seeds!
So I started working on the next section of the basement, at one end, clearing it out and mopping it. We have a low-to-the-ground twin size bed frame one of my nephews made that we painted and have been using for all sorts of things, inside and out. Once the end was mopped, I set it up under the counter was what was supposed to be a bar my late brother started building when he was in his teens and never quite finished. It has an outlet on the “outside” of the counter that we have found quite handy.
The bed frame is now set up under the counter, on bricks to keep it out of any water should we have issues again. I will be storing larger stuff on it, but made sure to plug an extension cord for us to use, as we won’t be able to access that outlet once the things are moved onto the bed frame.
The bed frame’s platform needed to be mopped, too.
After that was done, I set up a blower fan facing that end of the basement and am taking a break while it dries.
Oh! Break time is over! My brother is now here and in the old basement, figuring out how to set up the bypass valve so we can switch between the ejector and the emergency septic bypass. as needed – and not have to remove and switch pipes every time!
But no, the problem has not been fixed. In fact, it hasn’t even been identified.
When my brother got here, the first thing we did was see if the problem was with the pump itself.
I have learned a lot about this pump today!
The back valve was removed, and it was fine. Just a bit of gunk that would not have affected how it worked.
Since it was off anyhow, I gave it a thorough cleaning, along with the length of pipe and elbow that would be reattached to it.
From what we could see inside the back valve’s opening, the disc-type thing that would spin was also clear.
The pump has clean out valves, though. I had no idea what they were and couldn’t even see one of them without having to look around the outflow pipe from the filter. That was the next thing to check. Those have probably never been opened before, but my brother managed it. He took the bottom one out first, which was the drain, which is when we got a real hands on idea of just how much water is in that pump’s cannister section!
Trying to see into those openings was not easy. My brother got me to turn the pump’s switch on and off quickly, just so he could see things turning inside, using his phone as a flashlight. Everything looked fine. He did some cleaning around the thread and even poked around with a wire, but it was not all that gunky, either.
With everything checked and cleared, we tried again.
The pump ran, but no change. No water would flow.
Okay, maybe we just needed to prime the pump.
I had no idea there was a valve for that. As with the cleanout valves, it took a lot to get it open. Once it was, we used the hose I keep hooked up to the old laundry’s cold water tap all the time, because it’s just so handy. Once it was full, he closed it up again (making sure to Teflon tape everything, along the way), and we tested it again.
Nothing. No flow at all. The only change I could tell was that, with everything all nice and clean, the motor was running a bit quieter.
Okay, the pump seemed to be working. Could it be that something was blocking the tank’s outflow pipe?
There was only one thing left to do.
Put the emergency diverter back on.
If it worked after that, then we knew the problem was not at the house end.
Thankfully, when we switched it out before, I told my brother to just leave it aside. I would put it away in the spring, and then reseal the hole in the wall that it runs through. Which meant it was just a matter of switching pipes.
The outflow pipe from the pump to the ejector, however, always has water in it. It’s just a gravity thing. So we got a bucket handy before starting to take it off. As soon as my brother wrestled it loose, I got the bucket under it, so we did manage to catch most of it, but not all!
Yeah. I got splashed.
That out and set aside, the diverter was put back on. After double and triple checking that every thing was tight, we tried again.
Yes!!! It worked! Finally, the septic tank was draining!
My brother and I headed outside to check the other end, while my daughter stayed to monitor the pump. It emptied the tank and shut itself off before my brother and I could get to where it drains into!
Which means that the problem is somewhere from the house to the ejector.
We went to check the ejector.
The heat tape was not warm, but it has a regulator and will shut itself off based on temperature. Today has been a warm day, and is still warming up (as I write this, I see we just reached 0C/32F), so that makes sense. The extension cord’s plug has an indicator light on it, so we could see that it had power. Everything looked fine.
That doesn’t mean it’s not the ejector, though. It just means, we know it’s not frozen.
What it could be is that there is gunk in the venturi valve that finally just blocked the whole thing. The only way to know for sure is to pull it out. Which would require removing the heat tape, unscrewing the elbow at the top, unscrewing the cap, and removing both, then very carefully pulling the venturi pipe out of the stand pipe, so we can see the valve at the bottom.
Which we will NOT do until spring.
Yup. We’re on the emergency diverter for the rest of the winter, at least.
If it’s not the venturi valve being blocked, then it’s the pipe itself. A build up of crud inside the pipe could have come loose or something and blocked it entirely. Based on how well the water flowed out of the ejector after we got it thawed out and hooked up again, the pipe was running pretty clear. The only real hint that there was a problem was that it took longer for the pump to empty the tank than it did before.
There is nothing we can do about it until the ground thaws out.
Once the diverter was set up and working, my brother was prepared for another job.
Installing the power diverter switch.
The pump could be turned on and off using what is basically a light switch on the wall. Under normal circumstances this is in the “on” position at all times. The pump itself is triggered by the float and pill switch, inside the tank.
Sometimes, however, there is a need to check the pump, when the tank is not full enough to trigger it on. With all the septic problems we’ve been having, we needed to be able to turn it on manually, from inside the basement. The alternative would be to open up the septic can and use something long enough to catch the cable and raise the float. That’s something we want to avoid doing even in the summer. Not a chance, in the winter!
My brother set up a couple of wires set up outside the switch box that would allow us to turn it on manually. The pump’s switch would be turned off, the wires outside the box would be attached to each other, the switched turned on again, and the pump would run. When we were done testing it, we’d turn off the switch, undo the wires, cover and tuck them away again, then turn the switch back on so the pump could be triggered by the float again.
You can see the black covered wires from the pill switch coming up from below and into the box. The two wires sticking out the side from the same opening were the ones that could be joined to turn the pump on manually.
There was no schematic, so my brother had to be particularly careful in figuring out what was what. There were the wires from the breaker box (which was off, of course), the wires from the pill switch, the wires from the motor, the ground wires, and the manual diverter wires that all had to be kept track of!
He installed a new box, got all the wired sort out and attached to new switched, and put it all together, with one special feature, which you can see by clicking through to the next image (which Instagram, once again, messed with, so it’s off to once side instead of centred. *sigh*).
The manual switch has a safety cover on it, so that there is on way it can be turned on by accident!
Then he left the blue protective film on more me, because I commented on how I liked the blue colour. 😄
Of course, once everything was together – and before it was all closed up – the breaker was turned on and it was tested. I even made sure to get video of him explaining the which wires were which, so we can refer to it in the future, if need be.
My brother is so awesome. I don’t know what we would do without him! It even came up in our conversation today; my brother is the last living person who really knows this place. Another reason why I try to document everything, and learn as much as I can from him!!!
Once he was done with all this and his tools were safely put away and to the side, I did the floor pipe maintenance thing with the hose, showing him where I was hitting bottlenecks – except the second bottleneck wasn’t there! Or, at least, the hose passed through the opening just right, because he was there. 😄
Once that was done, I helped him haul all his tool boxes, bins and bags up and to his vehicle while my daughter, sweetheart that she is, took care of washing and disinfecting the floor. Mostly with one arm, since her ganglion is just not going away this time.
My brother may have finished up in the basement, but not with here! After loading up his car again, he went on to do things in their various storage areas for a couple more hours! Hopefully, the roads will be gone. We have just reached our high of the day; 2C/36F and are starting to get a bit of mixed rain and snow. We’re supposed to stay at this temperature through to tomorrow, even overnight.
Meanwhile, one of the first things I did was call dibs on the shower, after having been splashed while switching out that pipe. The honeypot has been put away, and we no longer have to use basins and buckets to keep water from draining into the full septic tank.
It feels so good to be able to shower again!
And use a flushing toilet instead of the honeypot.
At -27C/-17F, with a wind chill of -38C/-36F, my brother spent hours, here – most of it outdoors – getting things done.
The first thing was the no-longer frozen ejector.
When he arrived, he headed to the barn to get some stuff and I went out to join him. Along the way, I looked towards the ejector and got quite a surprise.
The tarp was gone, the sawhorse over the ejector was half knocked over, held in place only by the extension cord for the heat tape (safely secured), and the blue jugs from the liquid ice melter scattered in the snow nearby.
I don’t think my brother ever found the tarp. That part isn’t a surprise, considering the winds we had yesterday!
When we got to the basement, things there went quickly. The bypass wires on the switch was hooked up so that we could turn it on and off manually, rather than rely on the pill switch in the tank. The only difficult part was moving the emergency diverter off the pump without making too much of a mess. We knew there would be fluid in the pipe and I had a bucket ready, but there was just no way to get the diverter off and moved over the bucket without spilling at least some all over.
After the pipe to the ejector was put back, my brother and I fussed with our phones for a bit, so that we could communicate while he headed out to the ejector, then let me know to turn the pump on. We were able to make a video call, so when the time came, he had his phone set up so I could see the ejector.
The water flowing out of there was amazing! I’ve never seen it pushed out that far before (if I did when I was a child, I have no memory of it).
There was one odd thing about it, though. Instead of being pushed out in a steady stream, the bottom of the stream sprayed downwards, getting the stack pipe wet. My brother also saw water coming up from under the cap, which means the stack pipe was full, when it should have been drained by the venturi valve once water started to flow.
In the end, my brother found a piece of pipe he cut to create a little extender on the elbow piece.
He then dug around the barn and found bits and pieces to build a wind shelter around the ejector.
There’s a 1″ thick piece of rebar he hammered into the frozen ground to secure it, so the wind shouldn’t blow it away.
That rotten old sawhorse my brother dug out of the snow has sure come in handy!
All of this took at least a couple of hours, but we now have a working ejector again! No more emergency bypass draining the tank into the back yard!
The bypass is still there, though. I told my brother to leave it. I’ll take it out, put everything away and seal that opening up again, in the spring.
Then, before he left, my brother took care of a couple of other things, as well as going into their stored items.
Then he brought over one of his taller ladders.
Yup. He climbed up onto the roof to check the vent. The one warm day my daughters could have done it, one of them was in the city with me. The next day was the storm.
After clearing the area of snow, my brother ended up bringing a chimney sweep that’s stored in the barn to see if it was blocked. The non-sweep side could fit into the vent – and yes, it was quite blocked! I had a jug of hot water that he poured in, and the one jug was enough to clear it.
Meanwhile, I’d filled a sink with hot water to drain, so we could check if all was well.
All was well in the vent.
Not in the drain pipes!
The sink started to drain fine at first, and then it just sort of stopped. My daughter stayed in the kitchen to monitor while I went to the laundry drain.
Just in time to see the filthiest water coming out of there we’ve ever seen!
My daughter stopped the sink from draining. Thankfully, there was already a towel under the laundry drain, just in case, but it still took a while for the water to stop flowing. I was just heading out the door to tell my brother what happened when I heard something give, then gurgling as the water finally drained into the main pipe.
My brother thinks that the main problem is ice stuck in the pipe and suggested running hot water for a while. I suggested that clearing the vent knocked more gunk loose, too.
Thanks to the plumber installing the rubber connector in the pipe in the root cellar, this is something we can do ourselves. My brother had a few more things he wanted to do, plus take one last check on the pump (I had already taken care of the bypass and it was back to a pill switch trigger, instead of a manual trigger) before heading home. He told me that, as he was driving out here, he was seeing a vehicle in the ditch almost every mile of the way!
So we have had a major step forward, in that our septic system is up and running properly now – in fact, better than when we first moved here, thanks to getting that rag out of the back valve!
We had another step forward with my brother getting the ice out of the vent.
There’s just one step back, as our drain seems to be clogged again. We can use the kitchen sink, but it doesn’t take long before we can hear water backing up into the laundry drain.
That’s a job for this evening.
If all goes well, by the end of the day, we’ll be able to hook the washing machine discharge pipe into the drain again, and do laundry without running a hose out the door.
The important thing is, we can use our kitchen sink and laundry drain again! Yay!
We couldn’t wait until today to do our laundry, though, so yesterday we did something like four loads of laundry, with the hose draining out the door. The furthest end of the sump pump hose we’re using curls, preventing it from draining completely, so I kept going outside to lift the hose, from the door to the end, to get it empty before it froze.
This morning, we were expecting the plumber to arrive first, then a prescription delivery, hopefully before my daughter and I had to head out. My daughter had started her shower just as I was about to start heading outside for my morning rounds and to open the gate, when I heard a strange noise.
The septic pump had finally been triggered!
So I immediately dashed downstairs to check the filter.
Which was empty and running dry.
I shut the pump off, opened the filter, primed it again and turned the pump back on. It worked great! When it was done, the filter stayed full enough that the filter basket inside was floating and spinning slightly in the water – something I haven’t seen it do in quite a while!
From there, it was outside to feed and water the kitties, then do my usual checks, which this time included checking the outflow pipe. Everything looked clear, and there was no sign of backflow towards the house.
Yay!!!!
While doing my rounds, I got the truck running for a while, then popped in the OBDII scanner. The check engine light was on and the oil pressure gauge was still at zero. I did a full scan and got the same code as before: the oil pressure sensor that has already been replaced and cleaned.
At least it’s just triggering a check engine light, and not setting off the flipping alarm with the “turn off engine” warning.
From there, I cleared the codes and left the engine running until it shut itself off, as I’d used the remote starter to turn it on. Though it is much warmer today, I still plugged the block heater back in.
With our trip to the doctor’s office, though, I planned to use my brother’s car, which is parked and plugged in, outside. We had a bit of snow last night that needed to be brushed off, but that’s it.
Not long after I was back inside and checking the trail cam files, I got a call from the plumber. He was on his way and wanted to confirm directions to our place.
They can be a bit difficult to explain at times.
They got here soon after. Since the entry is where the laundry drain is, with the kitchen sink on the other side of the wall, I explained a what was going on there, then we went into the basement where I could show him the rest.
After looking over the pipes in old and new basements, as well as the plumbing under the sink, he decided to find a better way than trying to run his auger through where the last guy did. Access there is not easy, and it was put back together with adhesive. He didn’t want to cut anything there.
Since we knew the clog started past the laundry drain, he did it another way. He cut away part of the pipe in the root cellar, on the kitchen side of where the laundry pipe joined (not that he could have cut it on the other side, since it goes into a wall, there) and removed a couple of inches. It would then get sealed up with a rubber union and steel clamps, so that it would be easy to access, if we ever needed to have this done again. In fact, with our big drain auger, we’d be able to do it ourselves.
I don’t feel so bad about not trying to open things up where the other plumber went through now.
He used his smaller powered auger on the drain, and he really felt it when he hit the clog. After he worked on it for a while, with his assistant holding the other end of the pipe out of the way, he had his assistant go into the other basement to see if he could tell if the auger had reached the corner under the bathroom. I went along with him.
Not only had he reached the corner, but I could hear the tip of the auger rattling in the pipe near the old basement steps. He’d gone through the turn and was about 2/3s of the way down the other pipe to the septic tank.
After clearing things out, he sealed up the pipe, then headed for the kitchen to flush it. This will be our regular maintenance routine. He filled one of the kitchen sinks with straight hot water. After pulling the plug, he squirted some dish detergent into the vortex as it drained.
Then he did it again, with the other sink.
The first time, we could hear a lot of gurgling from the laundry drain pipe. A certain amount of that is normal, as we would be hearing the water pass by where it joined the main pipe. The second time he did it, we heard almost nothing from the laundry drain.
The assistant, meanwhile, was in the basement, making sure the new rubber union wasn’t leaking, and listening along the pipes. They couldn’t hear each other, so I went down and found him following the sound into the old basement. He could hear the water sloshing through the whole way.
I think the sinks were both filled and drained a total of three times each before he was satisfied.
I told him about what we’d found under the sink, and that my daughter had replaced everything but the trap, so he kept an eye on that, too. There were no leaks anywhere, so that was installed just fine.
While all this was going on, we chatted a fair bit. For some things, I explain the history of the plumbing, so far as I knew it. I even showed him our drain auger, and he quite approved. He let me know that, if we ever needed it, he does have a larger one. Hopefully, we never will!
He was one of the plumbers I have been talking to about the ejector, so while following the pipes, I showed him the diverter set up – and that the pump was triggered for the first time since the tank was emptied, just this morning. He was the one that has suggesting setting up an ice fishing tent over it with a heater, but we don’t even know someone we can borrow one from. He also suggested putting straw bales around the ejector, but we don’t have straw bales, either. We did get get straw, it was one of the big round bales, not the small square ones.
Oh, that reminds me…
While talking to the plumbing guy at the hardware store yesterday, we talked about the ejector and how to thaw it. He’s on an ejector system himself and said, this sometimes happen. I told him, it’s been some 50 years, and it’s never frozen before, so why now? He said it could be a few things and started listing some off. The only one I remember was when he said the ground could be saturated.
*dingdingding*
When they excavated down to the pipe to install the ejector, it was full of water. I even asked one of the guys if that was from the leaking old ejector, or if the water table was high. He told me it would be from the leaking ejector.
Which means the ground at the based of the new ejector was indeed saturated. Which would not have been a problem if this was done in the spring or summer. With nothing leaking anymore, it would have eventually drained away. The soil is clay heavy, so it might have taken a while, but it would eventually have dried up.
The ejector, however, was installed in… November? We were lucky not to have snow, which we did get, not long after.
Which means the water the drained to the bottom of the 4″ stack pipe had nowhere to go, and just kept building up and up, until it froze.
So… that rather eliminates any chance of us being able to use the ejector again until spring. The ground is already frozen, so even if we insulated around it, it wouldn’t make a difference.
*sigh*
We’ll figure it out.
The main thing is, we can now use our kitchen sink again!!!
In asking him why it would clog again so quickly after we’d already had it cleared just a couple of years ago, he said that having the laundry and kitchen drain into the main pipe so close together was not really an ideal situation. Between any grease from washing the dishes, to lint and such from the laundry, things build up pretty fast.
I’d been concerned about the pipe that didn’t get cleared, from the bathroom towards the septic. That, however, turns out not to be an issue at all. With all the water from showers and washing – even the toilet flushing – it would have kept that section of pipe pretty clear. There’s a lot less water running through from the kitchen to under the bathroom – and even less, when we started running the laundry drain outside. As the greasy water from the sink swirls its way down the pipe, the gunk would build up faster. Which is why flushing the drain with sink-fulls of hot water and detergent (he suggested using Dawn, as it is the best for grease cutting) regularly is recommended.
I asked him about using the bacteria and enzyme drain maintenance stuff, and he couldn’t really answer, as he doesn’t know much about it.
I also asked him about the possibility of the pipe from the house to the ejector getting clogged, and he said that was highly unlikely.
On top of all the other stuff we talked about, I mentioned that we want to replace the well pump, but there’s a risk of the foot valve breaking apart, so no one wanted to take the chance.
He pffffttt’d to that and said, just put in a check valve. No one really does foot valves anymore.
???
I’ve had three different plumbers look at that well pump. No one mentioned a check valve, so I asked him about it. He looked some up on his phone and found the style that would be used on our pump. He told me, just install that on the pump at the intake from the well, and don’t worry about the foot valve. Even if it breaks up, we’ll still get water.
I asked him, is this something that is new within the past few years?
Nope. They’ve been around for a while.
So now I wonder, why hasn’t any other plumber mentioned it??
Then, since we were walking around the three broken hot water tanks while looking around the basement, I told him about replacing the elements on the hot water tank recently, and what we found on the bottom. He told me, we need a water softening system to put a stop to that.
*sigh*
That’s something my husband has suggested, but a whole house system? That’s really expensive, and do we really want that for the entire house?
As to the cost, he was able to tell me that it’s $2500, installed, if he does it. He didn’t try to sell me on it; just let me know.
So all of that went fairly quickly. Before he left, I gave him my email address for him to send me the bill, so I still don’t know how much it will cost. I should get it tonight some time, but he told me that if I don’t, check my spam folder! That’s been happening a lot, lately, he told me.
That done, we can finally hook up the washing machine’s hose back to the drain pipe, but we haven’t done that, yet. Priority is catching up on dishes!
I wanted to head out early with my daughter for our appointment, but we still had the prescription delivery that I wanted to wait for first, so we could lock the gate behind us when we left. Not too long after the plumber left, someone used the washroom, and I heard the septic pump go off again. No surprise, considering how much hot water got flushed through the pipes!
I went down to check and…
It was running dry again.
I shut it off and primed the filter – the seal on that lid was quite tight – turned it on and it was working fine again. So fine, in fact, that it took only 2, maybe 2 1/2 minutes to drain the tank!
Hopefully, you won’t have to go to Instagram to wash this.
The moisture underneath is from the water used to prime the filter.
When it was done, the filter stayed nice and full. I paused to update my brother on it (I’d been keeping him up to date with the plumber the whole time, too). As I was doing that, I heard a strange noise from the filter.
You might need to turn up your volume to hear it. Somehow, there was air getting in.
I grabbed some paper towel and dried up everything around the filter and pipe joins, then watched and waited before checking them again. Everything was dry. There is no leak.
So what is happening???
One of the things I did a while back was put a brick and a very thin piece of Styrofoam under the filter to support the weight of the water in it. I ended up finding another thin piece to raise it up just a bit higher, so there is now no sag or play at all. I primed the filter again, and that bubbling did not happen again.
Were were good? I don’t know. But I did pass that on to my brother, too!
Not long after, the prescription delivery guy arrived, and my daughter and I were soon headed out to our appointments (after having to chase a kitten out from under my brother’s car!). We left early, making a brief stop in my mother’s town to pick up some lunch at the gas station – they had chicken kabobs available this time, which my daughter loves. Those sell out really fast, and they don’t seem to make more of them throughout the day. By the time we got to the clinic, we were only about 15 minutes early, so I’m glad we headed out when we did.
I went in first for my meet and greet. Her first question was whether or not I already had a doctor, and I explained about my previous doctor moving to another clinic, and having an interim doctor now. I’m sure she’d be fine to keep seeing me, but it’s just more convenient to have the same doctor as my daughter.
So this was mostly a question and answer session and I explained some of the issues I’ve been having, and she is now officially my doctor, too. I mentioned my painkillers just aren’t cutting it anymore, especially since I had to switch to acetaminophen. So I did get a prescription pain killer. I’d mentioned how bad the joint pain can get some days, where every joint in my body hurts. She asked me what supplements I was one, and I told her. She then recommended I go on a B complex instead of the B12 I’m on, as one of the other B vitamins should help me with the joint pain. She also told me to take double the recommended dose. I mentioned the Charlie horses I’ve been getting, but I have also run out of zinc, and suggested picking that up might take care of that, and she said yes. (I’ve also increased my salt intake, before I ran out of zinc, and that’s when the Charlie horses seemed to stop until just recently)
So once I was done, I went across the hall to the pharmacy to pick up the supplements while my daughter was seen next. Then I went to the grocery store that shared the parking lot and picked up a couple of small things we’d run out of at home. From there, I waited in the car for my daughter.
Which is when I got a test from my husband. He’s just picked up a call from the pharmacy for me. They’d received my prescription, and did I want to get it filled right away?
Talk about fast!
Of course, my husband had no idea what they were talking about, yet! So I called the pharmacy and said to go ahead and fill it, and that I’d likely pick it up tomorrow, since I was still in another town.
Then I got a message from my daughter clearing a calendar date in three weeks for another follow up appointment. So that was done, too.
My daughter got some adjusted medications and another prescription. Her bloodwork showed her to be vitamin D deficient. I wasn’t surprised by that. This is Canada, and it’s winter, after all! She has also been referred to an endocrinologist for her PCOS.
So tomorrow, we’ll both go into town to pick up our prescriptions.
This time, I plan to use the truck.
From there, we started for home. Along the way, we stopped in my mother’s town so I could go to a branch of my bank and take out cash, then we stopped at the home of the guy who empties our septic tank to pay our bill. With tip!
We made one more stop on the way back, at the post office. I wasn’t expecting any parcels yet, but there were a couple for my husband and some regular mail. The letter mail I’ve been waiting for since the strike delayed it, still isn’t in, though. This is getting ridiculous.
After that, we could finally head home. I’m sure glad for the longer days, as it wasn’t full dark, yet!
The first thing I did once we brought everything inside was do the evening cat feeding. My husband had let me know my mother had called (he does not answer calls from her), once I was settled, I checked her message. Apparently, when they delivered her new bubble packs, they didn’t deliver her inhaler. So I called her back and she told me her adjusted dose bubble packs were delivered, but there was no puffer. She then started going on about how it was a guy who delivered it this time, and she didn’t recognize him, etc. So I asked if she called the pharmacy to ask why it wasn’t there, and she said no, then tried to go back to talking about the delivery guy. I told her, she needed to call the pharmacy right away.
Which is when she asked if I could do it, because her English isn’t so good.
Ah. Okay!
Then she gave me the number, so I didn’t have to look it up.
The thing is, my mother’s doctor’s appointment was on Monday. Her prescriptions were delivered on Tuesday. Today is Thursday. Why didn’t she say anything on Tuesday??
So I called the pharmacy and quickly realized why my mother didn’t want to call herself. They have an automated answering service, which she has a hard time with at the best of times. With this one, after I made the first selection (after having to listen to a promo for vaccines first), it put me through another spiel for other choices. When I selected one of those, which turned out to be the wrong one. It took me to another and, as I was going through that, it started asking for things like the prescription number. WTF??? It did give the option to go back to a previous menus, and the net thing I knew, I was listening to the vaccine promo again.
I finally got to a real, live pharmacist.
They know be my now. 😄
When I explained what my mother had told me, the pharmacist said it was there. She’d put it in the bag herself.
I told her, my mother said it wasn’t, and she suggested it might be on the bottom of the bag, and described the box to me. It’s purple, so it would be easy to see!
I called my mother back and explained it should be in the bag with her bubble packs.
Oh! Let me go check.
It was there.
My mother had never looked in the bag. She had expected the delivery person to hand it to her seperately.
My mother was supposed to start her new bubble packs immediately, setting the current one aside, to be taken back to the pharmacy, so they could update the dose on one of her meds for her.
I didn’t get a chance to ask, but it sounds like she just kept using the same bubble pack instead of switching to the ones with the correct dosage in it.
*sigh*
I let her go, though, so she could go over the instructions for the inhaler.
I’m starting to wonder if she’s up to even using one.
Something I will have to follow up on.
Meanwhile…
This evening, I heard the septic pump go off again, so I went down to check. The filter was empty again! This time, however, I could see there was a very slow flow was water going in. It wasn’t running quite dry, but the flow from the tank was barely more than a splash. I stopped it and primed the filter again (it was tightly sealed), and it ran great after that. When it stopped, the filter was still full of water, and no sign of bubbles to show if there was some sort of air leak.
If this thing needs to be primed every time the pump goes off, that’s going to be a problem. I’m the only one that can hear it go off, and the camera I got to monitor it is going to be returned tomorrow, because it won’t connect to our WiFi.
This is incredibly frustrating.
If there is anyone more knowledgeable than me reading this and has some idea of what’s going on, please let me know! I’m running out of ideas.
As for me, I am done with this day.
I am so glad the plumber could come in this morning, and that we got that clog cleared. We learned a lot from him while he was here, too, and have steps to take to keep it from happening again – or at least keep it from happening again too soon!
I’m happy to learn about the check valve that would allow us to get that well pump changed and not worry about the foot valve.
I’m glad to finally and officially have a new doctor, and that my daughter got that referral to an endocrinologist, though it will likely take months before she actually sees one.
I’m glad the emergency diverter is working, even with the flow problems.
I’m thankful to have my brother’s car to drive today, even though it would have been just fine using the truck. I’m just paranoid about the truck. We need to get their car back to them soon.
I’m thankful for my other daughter’s financial help that paid for the septic guy, and is helping to pay for the plumber, too.
I may be done with this day, but it really was a very good day!
I did get one thing planned accomplished. While doing my morning rounds, I used the foil insulation in strategic points on the outflow pipe for our emergency septic diverter. The pump has still not been triggered to empty the grey water, so this will ensure any contact point with cold supports will not freeze.
Hopefully. At least, if it does freeze there, it would be much easier to deal with it.
Once my morning rounds were done and breakfast was had, my plan was to head outside and start searching for something we could use to shelter the frozen septic ejector.
Then one of my daughters came over to let me know the kitchen sink was clogged. They’d started doing dishes, and the skinks would not drain. They did eventually empty, but very, very slowly.
My younger daughter – the only one able bodied enough to do this – cleared things stored under the sink to check the pipes.
Note the big crack in the brass fitting above the trap.
There was no way to take the trap off to clear the clog (drain cleaner did not work) without the brass breaking even worse.
Which meant a trip into town to get replacement parts.
That left me in a bit of a conundrum. The truck’s sensor issues are still a problem. I’d been idling the engine to get it to warm up and evaporate the moisture that is triggering the sensor, but the truck really needs to be driven. But the oil pressure gauge is at 0, and that check engine light was back on after I’d cleared the codes, yesterday. I could have taken my brother’s car, but he’s going to need that back, and this sensor thing isn’t going to go away if I don’t actually drive the truck.
But we’ve had so many things got wrong, I was really uncomfortable doing it. The truck had started fine, the engine is running smoothly, and the oil levels are good.
I ended up texting our mechanic and asked him is he was sure it was safe to drive – and to please humour my paranoia! 😄 He said yes.
I had wanted to go into town anyhow, to refill our water jugs, so I grabbed those and headed out, with a brief stop at the post office along the way. The letter mail I am waiting for still isn’t in, but a couple of packages made it, so that was good, at least.
The truck ran fine the entire trip, too.
Once at the hardware store, I got to talk to my favourite person in the plumbing department. He’s been helping me a lot!
After showing him the pictures, he gave me the parts and pieces to replace the brass T, making sure to get me the correct adhesive and explaining about putting it all together dry, first, then taking it apart to use the adhesive. We were pretty sure of the size needed, but if we were wrong, I could return the parts and get the right size.
From there, I made a quick stop at the grocery store to refill the water jugs, grab some pumpernickel bread, as the rye was gone, and ended up getting some lactose free cheese for the girls that was on sale.
When I got back, my daughter set about taking out the brass T – which turned out to have a lot more damage than was visible – then removing the trap to clear the clog.
It got rather messy.
Along with the parts and pieces, I picked up a drain clearer -, I don’t remember the proper name for it, but it’s a long flexible wire with a plastic scrubby tuft at the end. I also picked up a sink plunger. My daughter took everything apart and used the drain clearer on the pipes for as far as she could reach with it.
That got messy, too!
Then she put the trap back and moved on to putting together the new T pieces and do a dry install to make sure everything fit.
They didn’t.
It fit at the top, directly to one sink, and the bottom, to the trap. It was the pipe to the other sink that was the problem. The brass T’s fitting was almost flush, as you can see in the above photo. The new T’s fittings extended further. There wasn’t enough play in the pipe to be able to attach the T to the copper pipe.
That bit of copper pipe, meanwhile, was basically jammed into a length of PVC pipe, likely with the use of a heat gun. My daughter hoped to push it further in, just half an inch, but it just would not move.
Which meant cutting the copper pipe.
The 1 1/2″ copper pipe.
We don’t have a pipe cutter to do it. We could have used a hack saw, but the very idea of trying to cut a pipe in a crowded space – on that wiggles around, at that – was not acceptable.
Time to go back into town.
While my daughter was fighting with the new T, I had taken the time to clean the threads on the trap and was thinking it would probably be a good idea to get a new one. Just in case.
So, off to town I went!
By this time, several hours had passed, so my husband requested I make another stop at the grocery store for some heat and eats. No one was going to be making a from-scratch meal, today, that’s for sure!
I also brought along the brass T to show the guy at the hardware store. When I got there, it turned out he’d stepped out for something. I waited a while, looking at things and, after clearing it with my husband first (since it was coming off his personal budget), I picked up an indoor/outdoor security camera that screws into a light bulb socket, and has an LED light built in as well. This would go in the light socket near the septic pump, so we could monitor it without having to go up and down those insane stairs all the time! It used WiFi and an app to control and monitor it, and had a slot for a micro SD card. We have a couple of those handy!
They didn’t know when the plumbing guy would be back, so after I got the security camera, I went to the grocery store. It turned out to be really busy, and I found out why when I was asked if I wanted to collect extra points, or get 10% off.
I took the 10% off.
The plumbing guy was there by the time I got back. I showed him the brass part, and then pictures of my daughter holding the new T that couldn’t join the copper pipe.
After seeing more of the photos and how the copper pipe was installed, he was rather taken aback. That’s a pretty big no-no, and he was trying to figure out what was holding it in place. I told him, probably just friction. Why wasn’t it leaking? he wondered. I told him, that thing is NOT moving. It is completely water tight, and likely inserted with the use of a heat gun.
One thing was sure, though. I was not going to find a pipe cutter for a pipe that size. If we wanted to shorten it, we’d need to use a hacksaw.
He asked more questions about where the pipe with the copper piece led to, and I told him is was to the second sink.
Well, that gave us a solution.
He showed me a kit for plumbing a double sink. All the parts and pieces I would need, plus a few extras that wouldn’t be needed for our particular set up. He even took it out of the package and assembled it for me, how it would go under the sinks.
I talked to him about the trap, as I’d been looking at one that had a clean out opening. He agreed that would be the best. The only potential issue was the elbow part of it that joined the outflow pipe to the main drain. That part is sealed with adhesive. The U part of the trap screws onto that part and, in theory, we could remove the take off the new elbow and screw the U part onto the existing elbow, but with how old these parts are, the threads might not be the same. If they weren’t, we’d have to cut off the elbow and adhere the new one; there should be enough play in the pipe to handle losing that half inch or so.
There was a fitting that would be needed that I already had, with the parts and pieces of the new T we would no longer need, but I went ahead and bought another one. Having extra parts is always good!
This guy is such a help! It’s great to have staff that knows their stuff so well.
From there, it was home again. By this time, my poor daughter was really struggling. She may be the most able bodied of us all, but she does have other issues! Her PCOS really does a number on her joints, and she was losing her ability to use one wrist. I had suggested taking a break to have food, but since the dishes hadn’t been done, due to the sink being clogged, things to use to cook with were unavailable.
Plus, she just wanted to get it over with!
So I left her to it for a while, after bringing her what she would need to trim the length of pipe between the sinks to the right side, then started setting up the new camera before heading to the basement.
Long story short, I will probably be returning it. It simply will not connect to our WiFi.
*sigh*
It’s possible it might work somewhere not in the basement, but I bought it specifically so I could monitor the septic pump and area, so there’s no point in keeping it if I can’t use it there. There is nowhere else we would want to set up a camera that works by screwing into a light fixture.
Meanwhile, my daughter finally got to the point where we could test the sinks and see if anything was leaking.
Since we’ve moved here, we’ve replaced both sink drains, and installed the flexible water pipes with build in shut off valves, replacing copper pipes with no shut off valves. Now, we’ve replaced the rest of the pipes under the sinks, up to, but not including the trap.
At some point, my daughter used the sink plunger. Apparently, it did an amazing job in clearing crud out.
As we were cleaning up and putting things away – it was full dark by this time – my daughter realized she was hearing splashing noises.
That test we did to see if there were any leaks?
The water had overflowed the washing machine drain in the entry, and was splashing all over the floor under the washing machine.
We grabbed a bunch of towels to soak up the mess as best we could without actually moving both the washer and drier (there is a single step just barely in front of the washing machine, so it can’t be pulled out without moving the drier).
My daughter decided to try using drain cleaner and poured some down the washing machine drain pipe – we have an extra long, flexible funny just to access this drain without having to move the washing machine. She set a times for half an hour, before boiling water would be poured down, then took a well deserved break.
I used that time to set up the basins to wash as rinse as many dishes as I could fit in the dish tray. Once that was done, the dirty water could be tossed outside, since we can’t drain anything down the kitchen sink, still.
Meanwhile, my daughter was able to set a couple of baking trays in the oven for some of what I’d picked up at the grocery store for them, now that access to the oven was no longer blocked by a took kit and all the stuff that had been stored under the sink.
My daughter finally got to eat, after about 14-15 hours.
While all this was going on, I kept my brother up to date. We are at a loss as to why this main drain pipe is so clogged. We had it routered 2 or 3 years ago. The first time it had ever been cleared in almost 50 years. Why is it clogged again after such a short time? And this badly! We’ve been trying to be diligent in making sure nothing goes down the drain that shouldn’t, like grease and whatnot, and using the bacteria and enzyme pipe maintenance stuff.
We do have that commercial drain auger my husband bought for me. We just don’t have what we need to be able to open up the main line in the basement, then seal it up again properly.
My brother wondered if it was possible there was freezing happening. The pipe runs past the old basement window. That window, however, is currently filled in with 3″ thick Styrofoam insulation on the inside, and on the outside, it has what used to be a “roof” above the window, now leaning over it for protection from the elements. That entire corner, on the outside, is well sheltered.
My husband’s bedroom is right above this area, though, and he says he can hear the gurgling in the pipes, and thinks the clog is near that window. He may be partially right. However…
After the drain cleaner got to sit for half an hour, my daughter went to pour boiling water down. She poured straight from the kettle, which is 1.7L
I don’t think she got more than a litre in before it started to overflow the pipe!
Which means the clog is practically at the bottom of the drain pipe.
This drain pipe has been here since the house got indoor plumbing in the mid 70’s. While there is a washing machine in the entry now, when the new part of the house was added on, my dad had a sink installed in the entry, so that they could wash up from working in the barn or whatever, before going into the rest of the house. Basically, it was a mud room. My mother apparently hated have a sink there, so when they stopped having cattle, she put something over the sink and taps, covered it with a cloth, and put decorative stuff on it.
I found the original sink, and the counter it’s in, in one of the sheds.
When my husband and younger daughter came out several weeks ahead of my older daughter and I, my younger daughter helped my brother turn the entry into a laundry room, taking advantage of the existing plumbing, so that we wouldn’t have to go up and down those horrible stairs carrying laundry all the time.
Have a mentioned, my brother is awesome?
He has also been asking me to take pictures of various parts of the plumbing to send to him. I have no intention of asking, but I suspect he plans to come out here to see what he can do. He needs to retrieve his car, anyhow, now that it seems our truck really is safe to drive and is running quite well, in spite of a sensor telling us otherwise. My brother knows how to do this stuff, and has the tools – but they are mostly here, and scattered in different areas.
The alternative is to call a plumber to clear that drain again. Last I looked, it was a flat rate of $300 for a drain clearing plus 1 hour of time. Parts and more time extra, if it turns out to be a bigger problem. That was a few years ago, and I expect the prices have had to go up, with how much more expensive things have gotten since then. I’ve tried calling that plumber a few times since then, left messages and never got return calls. We used this company because it was the only one that had the big drain auger – they cleared the floor pipe to the septic tank, the first time we called them. This time, though, we have our own auger, so really, we could call any plumber.
But not today.
After all that fighting with the kitchen plumbing – which did turn out to be necessary, considering the condition of things under there – we still can’t use our kitchen sink.
At least the line from the bathroom to where it drops down to the septic tank is clear!
I have no idea what we’re going to do at this point. Thankfully, my older daughter was able to help with covering the cost of vehicle repairs and paying the septic guy, but that can get used up awfully fast! Just the stuff I got today is only because she was able to help out.
As for me, I am just tired. Mentally tired. So very tired of things breaking down. It’s been more than a year of one thing after another, and even when things get fixed – like the ejector, or that sensor on the truck – it’s still an issue.
This is really starting to drain everything out of me.
Not that it matters. All we can do is keep chugging along, making do with what we have.
For now, that means things like doing the dishes in basins and dumping the water outside, and having an emergency diverter attached to our septic pump to also dump things outside.
I think I need to make myself go to bed early, and try to get some rest. Thankfully, I’m not the one that had to crawl around under a sink, so I didn’t have any major exertions. Just walking around with my brother as he was checking the expeller and installing the diverter did me in, unexpectedly. It has been a long time, but at about 3am last night, it caught up with me and I got hit with Charlie Horses again. This time, both thighs, all the way around. All I did was try to roll over in bed, and that was it. Thankfully, my daughters were up and heard me calling for help, and my younger daughter was able to bring me some ibuprofen (acetaminophen doesn’t help for Charlie Horses) and stay with me. The attack – and that’s exactly what it felt like – ended as quickly as it started, which was the weirdest sensation. After all this time, going to bed now feels as risky and driving the truck with that sensor issue!
Today, I needed to drive my mother to her doctor’s appointment, but didn’t have to leave until morning.
That gave me a chance to check on our emergency diverter set up that my brother made outside the house, ensuring that things were still sitting where they needed to.
Aside from making sure the PVC pipe my brother found was snug against the house, this is the important part.
The orange tarp partially buried in snow is the end of the insulated tarp covering the septic tank that we did not have to move. It was pulled away from the house, instead. This end gets frozen harder to the ground.
The two lengths of pipe need to be kept straight and slow downwards. At the bottom left corner of the above photo, you can just see the section of chimney flu that is supporting it closer to the house. We used basically what we could find in the dark. They will do the job, as long as things stay where they are supposed to. The shoveled area in the snow will basically become a skating rink.
In the distance, you can see the large flexible hose that was meant to be used. The problem is, it doesn’t straighten out entirely. Ever snake-like turn is an area that water could potentially slow down and freeze. The pipe is about 6″ in diameter, but even that can eventually fill and freeze solid. So it looks like we won’t be able to use it.
But I’m getting ahead of myself.
Using my brother’s car (and making sure to give the engine time to warm up, first!), I headed out early enough to hit the post office.
Alas, the mail that I’m expecting that didn’t come in due to the postal strike, still has not come in. Nor has anything else. Not even junk mail. The strikers may have been ordered to return to work (as a Crown corporation, the Federal government has the authority to do that), but apparently, that doesn’t mean they are going to actually do their work.
Oh, something I learned about this strike. It turns out that Canada Post has two unions. One is for the regular postal workers we see delivering our mail and in the physical buildings, like in our little hamlet. The other is for the ones that work in the distribution centres and such. Those are the ones that went on strike. So, while regular postal workers still showed up for work, they couldn’t do anything, because the distribution centres were shut down. It was a rotating strike, so every week, a different distribution centre would be active again, allowing for some mail to trickle through. Of course, if it was going from one distribution centre to the next, that really didn’t make much difference.
But I digress.
From there, it was off to my mother’s town and, since I was so early, I swung by the hardware store. After talking to one of the staff, I picked up some reflective insulation. They sell this stuff in sizes large enough to wrap around hot water tanks, to narrow strips that would be wrapped around pipes. Which is exactly what I wanted. I also got a small roll of aluminum tape. I plan to wrap the outflow pipe where it butts up against the house, as that is the area most at risk of freezing. Then I plan to add some between the pipes and the supports. Where the log is, isn’t much of a concern, but the ceramic chimney flu and the brick can both chill the pipe and potentially cause an ice build up on the inside. Just a bit of insulation would prevent that.
From there, I made a stop at the gas station. I didn’t need gas yet, but I knew my mother would be getting her Meals on Wheels today. Though I had a large and late breakfast before I left, she had told me she didn’t like to be eating by herself, with someone watching her. So I picked up some of the potato wedges she likes so much, so that I could snack while she was eating, and she could have the rest with her supper, later on.
When I got to her place, though, she had just finished eating her main meal. So we had some tea while she ate her desert. 😊 We were able to have a bit of a visit before we had to leave, and I updated her a bit on what was going on, and that my brother had lent us their car rather than my SIL driving all the way out to drive both of us around, and that he’d installed the diverter. I’m not sure, but I think she was still living at the farm the last time (and first time) it was used.
We left early to go to her doctor’s appointment, and I’m glad we did. I ended up having to go back to her apartment to get her little folding foot stool. Even though the car is so much lower than the truck, she still needed the stool to be able to get in! That is a definite drop in mobility.
Once at the clinic, we had a long wait, as everyone was being called in late. Once in the examination room, we still had a bit of a wait. When the doctor finally came in, she started off asking if we could move to another room, but then she saw my mother and told us to stay put, she would go get her laptop. It turns out the clinic was having network problems with all the examination room computers, and that was why everything was behind.
So we tried to keep it short. The main thing was to get my mother rescheduled for the MRI we didn’t get to, due to dangerous road conditions. I confirmed that my mother’s file was up to date about her macular degeneration and treatment. The doctor has nothing to do with this, as my mother is being treated at the eye clinic in the city, but as the primary doctor, she is supposed to have all this information sent to her. Then we talked about my mother’s breathing issues. One of her neighbours has asthma and uses a puffer (inhaler), so my mother decided she should have one, too. So could she be tested for asthma?
The doctor just prescribed her a puffer. She explained that she could recommend her for testing, but that is done in the city, and my mother would be on a waiting list for probably a year. Using a puffer won’t hurt her. I don’t think my mother as asthma, but even if there’s just a placebo effect, it would be worth it.
After giving my mother a basic physical exam, the doctor adjusted one of her dosages, and that was it. We knew the doctor was behind because of the computer issues, so we didn’t talk about much else. Which is good, because my mother usually wastes time by asking personal questions, or bringing up issues that she has… opinions on, shall we say.
My mother wasn’t due for any bloodwork, but the doctor did want to see her again in 3 months, so I made that appointment before we headed out.
Since the doctor faxed the new and updated prescriptions directly to the pharmacy in my mother’s town, that was our first stop. I went in while my mother stayed in the car, as it was just too much for her to go in and out. My mother was due to have her bubble packs delivered on Friday, and has started her last week’s current pack, so when I got there, her new packs were already there and ready to go. So that got pulled and adjusted for the new dosage. Instead of delivering on Friday, they will deliver tomorrow. As for the last pack my mother just started, the pharmacist said for her to set it aside and use the new once when they arrive, and the current pack can be brought back and adjusted.
As for the inhaler, it would take an hour before it would be ready, so that will be delivered tomorrow, too. Having been given an inhaler to see if it would help with my own respiratory issues (which we’ve never found the cause of, and I’ve basically given up trying to find one), I was able to explain to my mother how they work and how to use one, etc. She’ll need reminding, of course, but I hope the staff that delivers her meds tomorrow will be able to explain it again.
That done, there was just a brief stop at the grocery store for me to run in and pick up a couple of things for my mother before I took her home. I didn’t stay too much longer after that. I’m glad the days are longer, and I did manage to get home while it was still light out.
In between all this, I was able to send the OBDII scan results on the truck to the garage and he was able to respond. It’s basically the oil pressure sensor again. The one that was recently replaced, and also recently cleaned out because it was triggering the alarm and “shut off engine now” warnings, because it thought the truck was out of oil. This time, it has so far just turned on the check engine light again (though I did clear the codes, so that should be off now), and it why the oil pressure gauge isn’t moving. He told me, even if he replaced the sensor again, it’ll keep happening, because of the weather we’ve been having. There’s really nothing he can do about it. I suppose I could pay him to take it apart and clean it again, but that’s about it.
So really, what I need to be doing is getting the engine warmed up and staying warm long enough to evaporate any moisture in the system and triggering the sensor. It’ll resolve itself as things warm up again, as there won’t be that build up of moisture anymore.
I don’t need to go anywhere tomorrow, and it’s supposed to be a bit warmer, so I’ll run the engine while I’m outside.
Which leads me to my phone call with my brother this evening.
I’d sent the pictures he took to the company that installed the ejector, and the response was the same. The pump isn’t pushing out the water fast enough to create the pressure needed. This frustrated my brother to know end, because he knows the pump is pushing fine. As for how long it takes to drain the tank, he told me that 5 minutes is about right, because our tank is about twice the size of most other tanks. It’s huge. I was so young when it was installed, I was probably not allowed to go anywhere near it at the time.
Plus, that ice wall on the sheet of metal roof the ejector expels the water onto shows just how far and how strong the flow of water is.
Or was.
I know I’ve described the ejector system before, but my brother sent me some info with a diagram. The image was a pdf and terrible pixelated, but I think I got a decent screen cap of it.
I don’t know if ours is from this company, but it’s the exact same design.
With our new ejector, it’s about 2′ above ground, so about 8′ is below ground. I think the original was more like 12′ based on how much more was above ground than the new one. The venturi pipe – the discharge pipe, in the diagram – should never stay full once the pump shuts off. Once installed, the venturi pipe can be (carefully!) removed and replaced, which is what we were supposed to do after using enough hot water to thaw the ice and free it.
One of the things my brother brought up again was electric heat tape. There are all kinds of heat tape, and my husband had sent me a link for one that he’d found on Amazon. As my brother voiced concerns that, if we did try to use heat tape to thaw the above ground portion of the 4″ stand pipe, it might melt the plastic, I sent him the link. It is safe for both metal and plastic pipes, and self regulating. It’s also available in a huge range of lengths. He estimated that a 12′ length would be enough to wrap around the pipe, up to the elbow coming out of the cap. It was affordable, so I ordered it. It’s estimated to arrive on the 17th, though, so we have other things to try.
One of the things my brother thinks is a contributing factor is the new location of the ejector. The old one was about 10-15 feet away, and had a big willow overhanging it. The willow may have protected it from the elements (even though the roots were probably why it was starting to lean backwards and eventually start leaking). Right now, the ejector may be in full sunlight, but it is completely exposed to the winds we get. With the temperatures we’ve had lately, that could be a contributing factor so a slow freeze happening, and to the slow flow I was seeing in the filter. As long as some water was getting through, it wasn’t freezing completely, though, and just building up. I have a theory. The night before I discovered no flow was happening at all anymore, the septic pump had not gone off at all. Normally, between the 4 of us, plus my older daughter working at night, there’s plenty of toilet flushing, dish washing and even at least one shower. That didn’t happen, and it may have allowed for the stand pipe to finally freeze solid, and the venturi (discharge) pipe along with it.
I had already been thinking that, in the spring, I would need to put some sort of fence around the new ejector. Being so much lower to the ground, the renters cows out traipse right over it, even with the metal sheet butted up against it to divert the flow of water. My brother was thinking we’d need to build some kind of semi-permanent shelter over or around it, to protect it from the element in winter. I say “semi-permanent” as we need to assume that, some day, it will need to have work done on it, and we’d need to be able to move it.
At one point, I thought of the catio. It has a clear roof and is wrapped in plastic, making it almost a mini greenhouse. It would fit over the ejector.
Then I remembered the metal sheet. It couldn’t fit on top of that, since it has a curl to it that ensures the water flows away, and not off the sides.
But, there was possibilities.
So, while we wait for the heat tape to arrive, we need to see if we can find something we can use to build a shelter over it for this winter. My brother thinks a couple of pallets set up as a V around it, then something on top, would do the trick. We have no pallets, but he’s sure he brought some. There might also be some scrap plywood we could find somewhere.
Which means, I have a task for tomorrow. Going through the barn and sheds to see what I can find that could be used to build a shelter over the ejector. Just something we can slap together for now, but strong and heavy enough to not be blown over and destroyed by the wind. Ideally, I’d find something clear for a “roof” and add a little passive solar heat.
Trudging around outside will also give me a chance to get the truck running and see how it does! We’re warming up over the next few days, including the overnight lows, which should help, too. The day after tomorrow, my daughter and I have our joint appointment. It would be good if we could use our own truck and return my brother’s car! They really do need two vehicles.
Well, we’ll see how it goes. There’s not much else we can do!
Meanwhile, our septic tank still hasn’t filled enough to trigger the pump, so we still don’t know if the diverter will actually work, yet. It should work just fine. It’s just that we’ve had so many things breaking down for so long, now, I’m getting pretty paranoid about it all!